jellis4148
Well-Known Member
- Thread starter
- #31
The thing is it didn’t bottom out. Somehow I bent the ball joint as you can see in my previous post. The passenger side bolt is about the same and no issues. I could only use the first hole for the cotterpin on both bottom ones after torquing them to the 35 ft lbs. I honestly don’t know how this all happened. There is some wiggle on the bottom knuckle hole. Don’t got elongated as well. I’m just putting a new knuckle and two new ball joints in on that side. Just have to pay attention and make sure everything is solid. I’ve done all the install, and I could’ve swore everything was perfect last time. Obviously not, but I thought it was.That nut looks like it's very far down the threaded area of the shank. If the nut is still "tight", it's likely bottomed out on the thread runout, and the taper of the shank was not tight in the tapered bore. Check to see if you just ran out of thread when you disassemble it. There really should be a steel washer between a nut and an aluminum component. Not saying OE had a washer, but they should have. And in your case, the installer should have seen how far down the shank the nut was going and put in a thick washer to keep the nut from bottoming.
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